土工基础 ›› 2021, Vol. 35 ›› Issue (6): 674-681.

• 工程实录 • 上一篇    下一篇

大口径污水排海管顶管工作井施工力学效应分析

赖银波   

  1. (中交第三航务工程局有限公司厦门分公司,福建厦门 361003)
  • 收稿日期:2021-05-03 修回日期:2021-05-11 出版日期:2021-12-30 发布日期:2021-12-24
  • 作者简介:赖银波(1976-),男,工程师,研究方向为市政工程施工技术。
  • 基金资助:
    厦门市建设局科技项目(XJK-2019-1-4)

Mechanical Effect of Large Diameter Sewage Pipe Jacking Launching Shaft Construction

LAI Yinbo   

  1. (Xiamen Division, CCCC Third Harbor Engineering Co. Ltd., Xiamen 361003)
  • Received:2021-05-03 Revised:2021-05-11 Online:2021-12-30 Published:2021-12-24

摘要: 为研究邻近海域、高水位高渗透性砂层中顶管工作井深基坑开挖的力学效应,以厦门前埔污水处理厂排海管工程为依托,采用数值模拟及现场实测方法,研究基坑在开挖过程基坑的围护桩内力及变形、周边土体的应力及变形。结果表明:地表沉降区域主要分布在基坑长边外侧,累计极值不超过8.8 mm;咬合桩挡墙水平位移和弯矩极值分别为24.6 mm、852.0 kN·m,弯矩极值位置随着开挖底标高变动,斜撑的轴力较大,但均处于安全范围;值得注意的是,破除洞门前隔墙水平轴力最大值2 267 kN·m-1,破除洞门后洞顶和洞底局部形成应力集中,轴力达到4744 kN·m-1。最后,结合现场实测数据分析,随着开挖挡墙水平位移逐渐增大,且极值位置向下移动,通过现场有效控制,极值可从24.6 mm降低至18.6 mm。


关键词: 污水排海管, 顶管施工, 顶管工作井, 有限元分析, 现场实测

Abstract: This paper presents the case history of construction of sewer outfall project of Qianpu wastewater treatment plant in Xiamen. In order to evaluate the mechanical effect of a deep excavation for the pipe jacking launching shaft nearshore under high groundwater table in high permeability sand layer, the numerical simulation and field measurement methods were used to study the internal force and deformation of soldier piles as well as the surrounding soils during the excavation. The results show that, the surface settlement area is mainly distributed outside the long side of the excavated area, and the cumulative maximum deformation value is less than 8.8 mm; The maximum horizontal displacement and bending moment of the retaining wall are 24.6 mm and 852.0 kN·m, respectively. The location of the maximum bending moment varies with the excavation elevation, and the axial force of the diagonal brace is larger, but they are in the allowable stress range. It is worth noting that the maximum horizontal axial force is 2267 kN per meter when the partition wall in front of the tunnel portal is broken, and the stress concentration is formed at the top and bottom of the tunnel after the tunnel portal is broken, and the axial force reaches 4744 kN per meter. Finally, combined with the field measured data, with the excavation retaining wall horizontal displacement gradually increases, and the location of the maximum horizontal displacement moves downward, through the effective control on site, the maximum lateral deflection value can be reduced from 24.6 mm to 18.6 mm.


Key words: sewage outfall, pipe jacking installation, pipe jacking launching shaft, finite element analysis, field measurement

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