土工基础 ›› 2025, Vol. 39 ›› Issue (4): 507-512.

• 工程实录 •    下一篇

地下车库抗浮及筏板开裂渗水综合治理

刘伟超   

  1. (上海长凯岩土工程有限公司,上海 200093)
  • 收稿日期:2023-06-12 修回日期:2023-06-30 出版日期:2025-08-31 发布日期:2025-08-27
  • 作者简介:刘伟超(1991-),男,硕士,工程师,研究方向为地下工程、基坑围护、建筑加固纠偏、地下室泄水减压等。

Comprehensive Mitigation of Anti-Buoyancy and Raft Foundation Cracking and Water Seepage in an Underground Garage

LIU Weichao   

  1. (Shanghai Changkai Geotechnical Engineering Co. Ltd., Shanghai 200093)
  • Received:2023-06-12 Revised:2023-06-30 Online:2025-08-31 Published:2025-08-27

摘要: 山东某工程原有抗拔锚杆在遭遇“50年一遇”暴雨灾害情况下,大部分被拉断。导致地下车库大幅度上浮、筏板新增多条裂缝、筏板出现多处空鼓。迫切需要对地下车库进行修缮处理。针对此类问题,该工程采取“抗拔注浆锚杆+泄水减压系统+下柱墩注浆+裂缝修复”四者结合的综合治理方案。最终达到了“抗浮承载力恢复+泄水减压抗浮储备+筏板下空隙填充+筏板裂缝修复”的良好效果。不仅有效解决了原有结构抗浮失效、筏板脱空问题,更是最大程度上修复了筏板原有损伤。加固后筏板未发展新增裂缝,地面平整无渗水,治理效果良好。此种综合治理方案相辅相成、相互促进,加固效果显著,为相似工程设计提供了一种新思路。

关键词: 抗拔注浆锚杆, 泄水减压系统, 下柱墩注浆, 裂缝修复, 综合治理

Abstract: Under a “50-year return period” storm, most of the original anti-uplift ground anchors of a project in Shandong were pulled out. Resulting in a significant uplift of the underground garage structure, multiple locations found cracks at the raft foundations, and several hollow bulges were also observed at the raft foundations. There is an urgent need to repair the underground garage. In response to such hazards, the project adopts a comprehensive mitigation plan that combining “anti-buoyancy grouted ground anchor + drainage and water pressure relief system+pier cap grouting+crack repair”. Finally, the good effect of the “restoration of anti-buoyancy axial resistance+anti-buoyancy reservation for water releasing and pore pressure relief +filling of gaps under the raft foundation+ repairing cracks on the raft foundation” was achieved. Not only did it effectively solve the problems of anti-buoyancy failure of the original structure and raft foundation separation, but it also maximizes the repair of the original damage of the raft foundation. After the mitigation, no further cracking development was observed at the raft foundation, and the ground was flat without water seepage. The mitigation effect was satisfactory. This comprehensive mitigation plan complements and improves each other, and the reinforcement effect is significant. This provides a new approach for similar engineering design and has achieved significant economic and social benefits.

Key words: Anti-Buoyancy Grouted Ground Anchor, Water Level Reduction and Pressure Relief System, Pier Cap Injection, Crack Repair, Comprehensive Mitigations

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