土工基础 ›› 2020, Vol. 34 ›› Issue (5): 537-540.

• 工程实录 • 上一篇    下一篇

基坑失效后回填加固的工程实例

彭莹   

  1. (成都兴蜀勘察基础工程公司,成都 610072)
  • 收稿日期:2019-11-12 修回日期:2019-11-25 出版日期:2020-10-20 发布日期:2020-11-02
  • 作者简介:彭 莹(1989-),女,工程师,研究方向为基坑工程及地质灾害岩土工程设计。

Case History of Backfilling of a Failed Deep Excavation Project

PENG Ying   

  1. (Chengdu Xingshu Geotechnical Investigation and Foundation Co. Ltd., Chengdu 610072)
  • Received:2019-11-12 Revised:2019-11-25 Online:2020-10-20 Published:2020-11-02

摘要: 基坑由于某种原因超过设计年限,若无法及时回填,将对基坑工程安全性造成影响。以成都某停工基坑工程为例,该基坑支护的使用年限已超过设计使用期限约6年,未进行回填的基坑周边地面有裂缝、桩间喷射混凝土老化剥落、冠梁顶上放坡部分垮塌、已施工的预应力锚索及锚头有锈蚀变形、坑底土体生长大量植物等情况,该工程一直处于停工状态,为了保证基坑安全,通过设计斜撑加反压土的方式,基坑采用部分回填后,变形观测结果表明,采取回填反压加斜撑的措施能够有效控制基坑水平位移,保证基坑安全。 


关键词: 基坑加固;回填反压 ,

Abstract: The backfilling of an existing excavated foundation pit was required to address the safety concern since the design life of an exposed deep excavation was exceeded. This paper presents a case history of back filling of a fully excavated foundation pit with exposure of six (6) years. The observed distresses of this deep excavation were cracks behind the supporting structure; spalling of shotcrete covering the soldier piles; localized shallow failures on back slopes behind the reinforced concrete waler beams; rusted anchor and anchor plates and overgrown vegetation at the bottom of excavation. Since there were no anticipated further construction activities for this project, it was decided to backfill the excavated area using rakers and soil berms to provide back pressure. During the backfilling operation, the deformations of the existing supporting structure were monitored, and the monitoring results suggested that the method used in the backfilling was effective and the construction was safe.

Key words: Soil improvement for the Deep Excavation, Backfilling Backpressure

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