›› 2016, Vol. 30 ›› Issue (2): 164-167.

• 工程实录 • 上一篇    下一篇

富水软弱地层盾构掘进引起邻近砌体建筑物沉降研究

华志刚   

  1. (广州地铁设计研究院有限公司,广州 510010)
  • 收稿日期:2015-03-17 出版日期:2016-04-20 发布日期:2016-04-27
  • 作者简介:华志刚(1989-),男,助理工程师,研究方向为城市轨道交通、地下结构、岩土结构。

Settlement of Building Induced by the Adjacent Shielded Tunnel Excavation in the Saturated Weak Soils

HUA Zhigang   

  1. (Guangzhou Metro Design & Research Institute Co. Ltd., Guangzhou 510010)
  • Received:2015-03-17 Online:2016-04-20 Published:2016-04-27

摘要: 以苏州地铁4号线某区间隧道下穿一砌体结构建筑物为研究对象,对右线隧道(先掘进)、左线隧道(后掘进)地表和建筑物测点历时沉降及建筑物倾斜进行分析,得出富水软弱地层盾构施工对邻近砌体结构建筑物的影响规律。结果表明:盾构刀盘距测点约18~5 m时,测点会有超前沉降约-2 mm,距测点约5~0 m时测点上隆约0.5~1 mm,盾构到达并通过测点时沉降发展较快,盾构通过后1~2天沉降趋于稳定;富水软弱土体经扰动后沉降更不易控制;盾构停机会导致地表和建筑物沉降增加;砌体结构建筑物整体性差,盾构下穿砌体结构建筑物易产生较大的不均匀沉降,且侧穿引起建筑物倾斜较正下穿大。

关键词: 富水软弱地层, 盾构掘进, 砌体结构建筑物, 沉降

Abstract: This paper presents a case history of the shielded tunnel excavation in the saturated weak soils in Suzhou Metro #4 Line. The twin tunnel tubes were underneath a masonry building structure. During the tunnel excavation, the deflections at the ground surface and the building structure were monitored. The results indicate that, when the blade was in the range of 18 m to 5 m to the monitored point, a vertical settlement of 2 millimeters was observed. A ground heave of 0.5 ot 1.0 millimeter could be monitored when the shielded blade is zero to 5 meters to the survey point. A fast deformation rate was observed when the blade is reached the monitored point and the deformation became stable one or two days after the excavation. The settlement control would be different if the saturated weak soil were disturbed. An increase in settlement at the ground surface and the building if the shielded excavation was stopped. Due to its poor stiffness, large differential settlement was observed in the masonry building. If the tunnel was under one side of the masonry building, tilting in the building could be observed.

Key words: Saturated Weak Soils, Shielded Tunnel Excavation, Masonry Building, Settlement